西南石油大学学报(自然科学版) ›› 2011, Vol. 33 ›› Issue (4): 169-172.DOI: 10.3863/j.issn.1674 – 5086.2011.04.032

• 石油机械工程及其他 • 上一篇    下一篇

AT21X 井 177.8 mm 尾管固井技术研究

陆长青   

  1. 中国石化华东石油局固井工程公司, 江苏 扬州 225101
  • 收稿日期:1900-01-01 修回日期:1900-01-01 出版日期:2011-08-20 发布日期:2011-08-20

177.8 mm Liner Cementing Technology in Well AT21X

LU Chang-qing   

  1. Cementing Engineering Department, East-China Petroleum Administration Bureau, SINOPEC, Yangzhou, Jiangsu 225101, China
  • Received:1900-01-01 Revised:1900-01-01 Online:2011-08-20 Published:2011-08-20

摘要: 塔河油田阿探区块的 AT21X 井采用 177.8 mm 尾管固井, 由于含盐、 井深、 井底温度高, 氯根离子含
量高, 井身结构特殊等原因, 固井作业困难。在井段采用两凝体系固井液, 在水泥浆中加入 2.0% 微硅和
0.2%TAS153, 很好地解决了盐膏层固井遇到的高温、 高盐、 易窜槽和易失水的问题, 改善了水泥浆的性能,
提高了固井质量。经检测固井合格率 100%, 其中优良率达到 90%, 固井质量综合为优秀。

关键词: 盐层, 尾管固井, 水泥浆, 固井技术, 前置液

Abstract: Well AT21X, which is an ultra-deep exploration well in Tahe Oilfield, adopts the ϕ 177.8 mm liner
cementing. The cementing operation is difficult owning to the deep depth, high temperature in the bottom hole,
high content of chloride ions and special well-structure. During the cementing, two slurries of different setting
times were used. In the slurries, 2% micro-silicon and 0.2% TAS153 were used to solve the problems caused by
the high temperature, high salt content, easy channeling and high water-loss when cementing an interval containing
salt formation. So the performances of cement slurries were improved as well as the cementing quality. Cementing
quality test result is that 100% cemented intervals are qualified, 90% good and excellent. The cementing technique
used provides a good example and some useful experiences, and can bring some guidance for the future cementing
operations concerning salt formation.

Key words: salt formation, liner cementing, cement slurry, cementing technology, pre-flushes

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